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POTENTIAL FAILURE MODES AND EFFECTS WORKSHEET
FMEA Type Level of Detail
Design FMEA Process FMEA System Process Process Step Component / Part FMEA Number ---> 5637-2007
Telephone #: Email address:
Product / Service 345-474494-8475 Design or Process Responsibility Alleak Valves Prepared by ---> Carl Spackler
Identifier ---> -------------> 585-555-1212 test@info.com
End Product(s) / Model RL-1500 Series Valves Other relevant information ---> None Original Date ---> May 29, 2007 FMEA Revision Date October 2, 2007
Year(s) ---> ------>
Core Team ---> Eric Cartman (FMEA Owner), Kenny (Plant Mfg. rep.), Stan Marsh (engineering rep.), Kyle Brovlowski (quality rep.), Mr. Garrison (purchasing / supplier quality rep.), Mr. Hand (Internal Customer rep.), Chef (Customer rep.)
S T Fishbone O D R S O D R
Design Item or Process Potential Failure Mode Potential Effect(s) of Failure e y Potential Cause(s) / Cause c Current Process Controls - Current Process Controls - e P Recommended Actions Responsibility & Target Actions Taken e c e P
Function Requirements v p Mechanism(s) of Failure Category c Prevention Detection t N Completion Date v c t N
e
saw cutting of tube wrong length cut regulatory violation 9 I wrong setup of saw method 3 setup programs 1st piece verification 3 81
9 I tube not fully held against method 5 OJT sensor on back stop with 2 90
back stop alarm
9 I method 0 0 0
I operator not trained properly man OJT process verifies Training records
9 4 competence through 4 144
testing
9 I operator tired or man 3 regular breaks / table regular supervisor visits 5 135
uncomfortable height can be adjusted
9 I operator distracted man 4 5 S program regular supervisor visits 5 180
9 I dull saw blade machine 3 PM checks every 1000 SPC checks every 2 hours 5 135
cuts
9 I wrong saw RPM machine 3 setup programs 1st piece verification 3 81
I backstop becomes loose machine OJT SPC checks every 2 hours Improve clamp on backstop Stan Marsh - 9/07 clamp improved and
9 7 5 315 and add sensor to detect sensor installed 9 3 2 54
movement
9 I tube straightness out of material 2 Supplier approval Cpk of CofA verified at incoming 7 126
specification 1.8 inspection
I Tube hardness out of material Supplier approval Cpk of .8 CofA verified at incoming Initiate supplier corrective Mr. Garrison - 9/07 CA completed and Cpk
9 specification 7 inspection 7 441 action and development to improved to 1.4 9 3 7 189
improve Cpk
I material expansion material temperature controlled in alarm system on
9 4 manufacturing to 68 +/- 5 temperature gage / 2 72
recorder
9 I unorganized work area environment 2 5S Program weekly 5S audits 5 90
I excessive dirt, dust or metal environment OJT regular supervisor visits
9 filings on saw cut table / 5 5 225
back stop
I temperature out of environment PM checks monthly - alarm system on
9 specification 3 stability of gage temperature gage / 2 54
recorder
I backstop not setup properly - measurement OJT 1st piece verification
9 measurement error 5 3 135
I gaging out of calibration measurement calibration frequency SPC checks every 2 hours
appropriate and methods
9 2 are capable - stability 5 90
studies
I SPC checks not being done measurement OJT regular supervisor visits -
supervisor is required to
9 5 verify SPC checks - 5 225
sampling
Printed: 08/03/2022 Page 1 of 1 FMEA Template Revision: 29-May-07
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